Change from Grizzly to LHD Extraction System

- Organization:
- The American Institute of Mining, Metallurgical, and Petroleum Engineers
- Pages:
- 12
- File Size:
- 592 KB
- Publication Date:
- Jan 1, 1981
Abstract
GENERAL OUTLINE For more than one hundred years, asbestos ore has been mined on Les Mines d’Amiante Bell's property at Thetford-Mines , Quebec, Canada. In 1878, the first tons of fibre were produced. The mine operated as an open pit until 1951 at a yearly production of about 330 000 mt of ore. Since 1951, the mine has operated underground using a block caving method. The mine produced 725 000 mt per year until 1978, when the rate of production was increased to 1 100 000 mt. The ore was produced entirely fm the first lift on 650 level until 1976. Then, a second lift on 950 level was put into operation to replace production facilities fm the first lift which is now exhausted. Annual fibre production is 72 500 mt with grades £ran 3 to 7. The total work force is 600 people. The host rock is a peridotite partially serpentinized. The asbestos fibre seams occur as stockwork deposit structurally controlled by talcose shear zone. The geological rock formations are heavily jointed and have a wide range of competence. Asbestos ore bodies have an heterogeneous nature which des difficult geological interpretation. THE GRIZZLY METHODS A full gravity method was used on the first level where the caved ore was drawn from finger raises onto grizzly bars spaced at 480 mn. Oversize blocks were reduced by secondary blasting. The ore fell by gravity in- to the ore pass below the grizzly chamber and was loaded into 5.7 mt haulage cars through a 1.2 m wide chute. Access to the undercut drift was fm the grizzly drift through finger raises. The undercut trough was drilled and blasted in a 1.2 m interval ring sequence into a slot situated at the end of each panel. The undercut stope was emptied through the finger raises. The undercut retreated from South to North at blast interval determined by the finger raises spacing. Fig. 1 represents the various steps involved with the grizzly method. Extraction drift dimensions were opened 1.8 m wide x 2.4 m high with anchor rock bolts and wire mesh where safety required them during excavation. Grizzly chambers were excavated at 2.4 x 2.4 x 4.6 m long on a 7.6 x 7.6 m grid spacing. Ore passes with dimensions of 1.5 x 1.5 m were developed from the haulage drift. On the extraction level, headings were drilled with jacklegs and cleaned by slusher into ore passes to the haulage chutes. The support used in the grizzly chambers was square concrete structure with 150 mn H beam reinforcement. The H beam was partially buried in the concrete and had one free face to allow for difference frequency of blast vibration between concrete and steel. The supported brow of the chamber had an opening 1.5 x 2.1 m. Ore passes were ring concreted 150 mn thick without any reinforcement. A 24 MPa compressive strength concrete was pumped and poured in pre-assembled forms. Based on the success of this method on the first level, the same layout was repeated on the second level. With the start of undercutting on the second lift, signs of deterioration were noticed in extraction drifts. At first, there was great concern as the operators were confident that standard repair techniques could cope with such a situation. An intensive program of support repair and a reduction of draw resulted. The following method of repairs were used: 1) Steel square sets of 150 mn H beam at 0.6 m intervals were installed. 2) This was reduced later to 0.3 m interval and eventually to a skin to skin steel structure. 3) Yieldable arches were introduced spaced at 0.9 m intervals, linked laterally with 150 m. H beam. 4) The yieldable arches spacing was then reduced to 0.46 m and eventually installed skin to skin. However, this support was not successful.
Citation
APA:
(1981) Change from Grizzly to LHD Extraction SystemMLA: Change from Grizzly to LHD Extraction System. The American Institute of Mining, Metallurgical, and Petroleum Engineers, 1981.