Minerals Beneficiation - Control of an Autogenous Grinding Circuit by Means o? a Crusher

- Organization:
- The American Institute of Mining, Metallurgical, and Petroleum Engineers
- Pages:
- 5
- File Size:
- 1699 KB
- Publication Date:
- Jan 1, 1971
Abstract
In single-stage autogenous grinding, the buildup of a critical size fraction in the media can be corrected by removing this material through pebble ports, crushing it below the critical size range, and recycling the crusher product back to the mill. The rate at which the critical sire fraction is crushed affects the size distribution of the grinding media and this in turn affects the sire distribution of the grate discharge. This provides a means for controlling the grind produced by a single-stage autogenous grinding unit. The pilot-plant investigations on a very hard copper ore were carried out at the facilities of the Institute of Mineral Research, Michigan Technological University. In an autogenous grinding circuit in which feed at approximately 9 in. top size is reduced to a size suitable for subsequent processing, the build-up of a "critical size" fraction in the media causes problems. A "critical size" fraction has been defined as, "media too small to effect reduction by impact grinding of ore coarser than a quarter of an inch and too large to be broken by the largest size of media in the charge."' The buildup of a critical size fraction reduces the capacity of the mill, increases the grinding power requirements per ton of finished product, and generally produces a finer grind than is desired. It is general practice to overcome this problem by the addition of large-diameter steel balls to the grinding charge. This has certain disadvantages, such as 1) an increase in mill liner wear, 2) wear on the steel balls, and 3) some loss in flexibility in grinding circuit opera-tions resulting from difficulties in removing the steel balls by means other than by grinding out. A number of investigators' have suggested the use of a small crusher as an alternative to the use of large steel balls for control of a critical size fraction. With this technique the critical size fraction is removed from the mill continuously through suitable-sized pebble ports, crushed below the critical size range, and returned to the mill. An external crusher would cause no increase in mill liner wear, the wear on the crusher would be less expensive than the wear on the steel balls, and the flexibility of the grinding circuit operations would be enhanced since the crusher can be cut into and out of the circuit at will. This paper describes an autogenous grinding pilot plant investigation on a very hard copper ore, which led to the selection of an autogenous grinding flowsheet incorporating a crusher in the circuit as the preferred method for grinding this ore. Further development of the technique demonstrated that the crusher could be employed to control the product produced by an autogenous grinding unit. Description of Pilot Plant These investigations were carried out at the pilot-plant facilities of the Institute of Mineral Research, Michigan Technological University, Houghton, Mich. The autogenous grinding unit was a 6-ft-diam by 2-ft-long Hardinge Cascade mill with %-in. slotted steel grates. Pebble ports cut into the grates allowed passage of pebbles having a top size of approximately 21/2 in. The grate and pebble-port discharge material passed over a 3/16-in, trommel screen with the trommel under -size being pumped to the classification device. DSM screens were employed for classification in the early investigations, but were replaced later by a small Dorr rake classifier. The trommel oversize material returned to the mill via scissor conveyors. When the crusher was incorporated into the circuit, the trommel oversize material passed to a double-deck vibrating screen fitted with 2-in. and 3/4-in. square mesh screen cloths. The $ 2-in. and the —2 +3/4-in. size fractions were combined and crushed to a nominal 1 in. in a 4 x 6-in. jaw crusher. The crusher discharge and the —3/4-in. screen undersize returned to the mill. In the final investigation, a flap gate fitted to the top deck of the screen directed the — 21/2 +2-in. size fraction to the crusher or back to the grinding mill. The flap gate operated manually on a 15-min cycle, with this material being crushed for so many minutes out of each cycle. This was found to be a more reliable method of controlling the amount of — 21/2 +2-in. material crushed than attempting to make a split of a small weight of material on a continuous basis. Operational Techniques: Each sample was sized into three fractions and the Cascade mill feed was reconstituted from these size fractions in the proportions existing in the original sample. Sufficient feed for 15 min operation was weighed out and fed by hand over a 15-min period. The gross mill power draft was recorded every 15 min, corrected for tare power and drive efficiency, and reported as net kilowatt-hours per ton. A recording kilo-watt-hour meter provided a continuous visual record of the power drawn by the mill. Pulp densities of the trommel undersize and the classifier overflow (or DSM undersize) were taken every 15 min. The classifier overflow was sampled automatically. Timed samples of the classifier sands were taken every 15 or 30 min, weighed, and returned to the circuit. After correcting for moisture content, the weights were converted into percent circulating load. Timed samples of the +2 in., the —2 + 3/4-in., —3/4-in. screen fractions, and the crusher discharge, were
Citation
APA:
(1971) Minerals Beneficiation - Control of an Autogenous Grinding Circuit by Means o? a CrusherMLA: Minerals Beneficiation - Control of an Autogenous Grinding Circuit by Means o? a Crusher. The American Institute of Mining, Metallurgical, and Petroleum Engineers, 1971.