Water Management And Control United Nuclear Corporation Church Rock Mill Practice

- Organization:
- The American Institute of Mining, Metallurgical, and Petroleum Engineers
- Pages:
- 8
- File Size:
- 466 KB
- Publication Date:
- Jan 1, 1982
Abstract
INTRODUCTION The idea of water management and control at the Church Rock Mill operations began to take shape in February 1979. At that time, we were already investigating the feasibility of decreasing the fresh water requirements so that the solids would become the limiting factor in tailings impoundment utilization. The area for solution evaporation could be kept at a fraction of the normal requirements under the standard process of full water usage. The Church Rock Mill is an acid leach circuit followed by solids/liquid separation with thickeners in counter current decantation, and solvent extraction. Following the normal design of acid leach circuits, reuse of tailings solution was not incorporated in the original mill process design. INITIAL WATER CONTROL INVESTIGATIONS The investigations to decrease the fresh water requirements centered around modifying the grinding circuit from the present semi-autogenous grinding (SAG) mill in closed circuit with hydrocyclones, to open circuit grinding with a rod mill. The open circuit grinding with the SAG mill and rod mill in series had the potential of decreasing the water requirements for grinding and leach dilution by approximately 50% or 1.4 m3/min (300 gpm). The grinding pulp density would be maintained at 70 to 72% solids, and the leach dilution to 50% solids would be accomplished with acid tailings liquor recycle. In such a grinding circuit arrangement, the SAG mill would provide the primary or coarse grind, and the rod mill would be used for the fine grind. By the SAG mill and rod mill series grinding method of water control and other secondary water controls in various places downstream from the grinding circuit, the required necessary evaporation area was estimated at 120 acres of liquid surface. A second method of water control at grinding was investigated. A two-stage cyclone classification circuit appeared to have a good potential of achieving the same water reduction at a much lower capital and operating cost. However, in retrospect, this would not have been a viable method since a high slime recycle load would have been established hindering classification. The use of reagents to neutralize the acid tailings solution was not considered seriously at that time, since it would have materially increased operating costs, although it would have also allowed more tailings solution recycle and consequently, less fresh water usage. However, with the tailings solution deposition area available at that time, it was not then necessary to incur the high cost of neutralization. The control expected by the series grinding of semiautogenous and rod mills would have been sufficient to maintain a water consumption/evaporation equilibrium well in line with the available land area. IMPLEMENTATION OF NEUTRALIZATION OPERATIONS During the summer of 1979, the UNC Church Rock Mill experienced a tailings dam breach which resulted in a prolonged mill shutdown. Upon resumption of operations at the end of October 1979, tailings deposition was restricted to a small portion of the tailings impoundment area. Figure 1 shows the general tailings area and the limits of the present deposition area in the central part including the borrow pits. These borrow pits had been excavated to provide materials for tailings dam construction. Immediately after resumption of operations, it became evident that it would be necessary to control the quantity of liquid to be evaporated because of the small confined area available for tailings solution deposition and to maximize the deposition time in the tailings area. The water control required had to be exercised on a large scale, and to be in operation as quickly as possible. An obvious solution was to reuse the tailings liquor in mill process. Immediate steps were taken to install the necessary equipment for tailings neutralization on an interim basis. Anhydrous ammonia was selected as the primary neutralization reagent since it was the quickest system that could be placed in operation. Previous laboratory tests indicated fair results with ammonia neutralization. Such a system required a minimum of installed equipment and handling. INITIAL NEUTRALIZATION OPERATIONS Actual neutralization operations began on November 26, 1979. The raffinate solution which normally would have been discarded was pumped to a 3.7 m (12ft) diam by 4.3 m (14ft) tank for reagent contact, see Figure 2. At this tank, anhydrous ammonia was added directly from the tanker trailers and controlled at pH 7.0 nominally. Agitation was provided by air sparging. The neutralized product formed a highly viscous slurry in the grinding circuit which resulted in pumping and cyclone classification problems.
Citation
APA:
(1982) Water Management And Control United Nuclear Corporation Church Rock Mill PracticeMLA: Water Management And Control United Nuclear Corporation Church Rock Mill Practice. The American Institute of Mining, Metallurgical, and Petroleum Engineers, 1982.