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Changing Borehole Length to Improve Breakage: a Case HistoryBy Norman S. Smith, Richard L. Ash
Many factors affect rock fragmentation from blasting. One variable seldom considered when designing blasts, however, is the borehole length. An example is described of how the length was adjusted to g
Jan 1, 1976
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The improvement of wear resistance by ion implantationBy R. Hutchings
The paper reviews current understanding of the effect of ion implantation on the wear process, and the state-of-the-art of ion implantation as a commercially viable treatment to impart wear resistance
Jan 1, 1986
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IC 6248 Methods And Costs Of Stripping And Mining At The United Verde Open-Pit Mine, Jerome, Ariz. ? IntroductionBy E. M. J. Alenius
This paper describing the mining practices at the United Verde open-pit mine at Jerome, Ariz., is one of a series being prepared by the United States Bureau of Mines on mining practices, methods, and
Jan 1, 1930
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Ground Improvement Resulting From Installation Of Drilled Displacement PilesBy Timothy C. Siegel
Drilled displacement piles (also known as augered cast-in-place displacement piles or augured, pressure grouted displacement piles) are installed by the displacement of soil and subsequent placement o
Jan 1, 2007
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Automated Process Control Improves Productivity at Asarco’s Mission ComplexBy Jack Garrity
The Asarco Mission Complex includes two milling operations around a large open-pit copper mine in southern Arizona. The ore body was discovered in 1953 and the complex has been in operation since 1959
Jan 1, 1995
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Government Policy And The Potash Industry In Saskatchewan ? IntroductionBy Arne Paus-Jenssen
The potash industry in Saskatchewan has recently been the focus of much new legislation at the provincial level and, along with other mining industries in Canada, also subject to changes in tax legisl
Jan 1, 1976
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The improved flotation of gold from the residues of Orange Free State oresBy P. A. J. Cabassi, B. K. Loveday, M. J. Wilkinson, P. H. Radcliffe
The recovery of gold, uranium, and pyrite from accumulated residues at mines in the Orange Free State is adversely affected by the presence of pyrophyllite, which is naturally floatable and must be pr
Jan 1, 1983
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Hole Cleaning Improvements through Tricone Bit Lug DesignBy Clarence Zink
Aside from the mechanical properties and process of actual rock breakage, rotary drill bit performance is affected by several “post breakage” items: cuttings size, flushing air pressure, flushing air
Jan 1, 2006
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Selective Flocculation of Apatite to Improve Flotation of Fine Phosphate Ore FractionsBy Y. H. Zhan
In beneficiation of phosphate ores it is common to use screening to produce the coarse "pebble" concentrate, and flotation to process the -1+0.1 mm size fraction. The -0.1 mm desliming product is trea
Jan 1, 2002
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Chicago Paper - Improved Slag-Pots (See Discussion. p . 675)By H. A. Keller
(Chicago Meeting, being part of the International Engineering Congress, August, 1803.) Among the important implements of most of our Western lead and copper smelting-works is the slag-cart or buggy
Jan 1, 1894
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Deteriorating Ground Conditions Lead To Improved Excavation And Ground Support Techniques At The Cantung MineBy W. J. Fotheringham
This paper deals with the mining techniques employed at Canada Tungsten's northern Canadian operations, particularly with respect to their effect on productivity, safety, and stability of relativ
Jan 1, 1985
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Hydraulic Tailing Fill Improvements - Butte-1969By Harold F. Yde
Hydraulic tailing fill in the Butte deep-level mines resulted from studies made in 1958 by The Anaconda Co. Mining Research Department. At the time of the study, dry mine tailing was hauled via rail c
Jan 1, 1970
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Crushing Flowsheet Simulation: Increased Productivity and Improved Flowsheet DesignBy K. Bryan, O&apos
A 10-year program to integrate crushing and screening models into daily flowsheet design practice has proven successful. A Circuit Analysis Program (CAP) is used worldwide to design and evaluate new a
Jan 1, 1987
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Improved Mining Economics Using Near-Face DeshalingBy G. T. Lineberry, R. Q. Honaker
Coal extraction typically results in the recovery of pure rock that ranges from small to very large quantities depending on seam thickness and other characteristics. The removal of pure rock may allo
Jan 1, 2004
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Improvements In Exploration Programs And Presentation Of Geotechnical Information: Program Management Approach, Milwaukee Water Pollution Abatement ProgramBy William B. Thayer, James H. Meinholz
The Milwaukee Metropolitan Sewerage District (MMSD) has been working since mid-1977 on a fast track to meet a court-imposed schedule to rehabilitate a large wastewater collection and treatment system
Jan 1, 1983
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Statistical Approach To Using Metallurgical Data To Improve The Accuracy And Information Obtained From Financial AnalysesBy Ross W. Smith, D. L. Taylor, K. A. Altman
Traditional sensitivity analysis of metallurgical data has the potential to overestimate the value of mining projects. Such analyses provide no information about the probability of the results. Simula
Jan 1, 2003
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Improved Safety and Operating Efficiency With Sound-Powered PhonesBy Robert W. Edwards
The Morris mine, operated by the Inland Steel Co., is located about 5 miles west of Ishpeming, Mich., near the west end of the Marquette Range. The ore, a soft hematite, is mined by sublevel caving an
Nov 1, 1955
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Reduction of Airborne Dust on the E48 Extraction Level at Northparkes MinesBy C Vejrazka, A Wyllie
A common problem faced by underground mining operations around the world is airborne dust sourced from production and auxiliary processes. In most underground mining methods, air is generally directed
Mar 24, 2014
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Technical Improvement And Modification Of Guixi Smelter In Recent Ten YearsBy Yuan Zeping
The Guixi smelter is the first Outokumpu flash smelter in China .It was commissioned on December 31, 1985. Originally, the smelter was designed to produce 90,000 tonnes of copper annually. After the i
Jan 1, 1999
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Improvement of the OPAP Uranium Recovery Process from Phosphoric AcidBy M. S. Tsai, Y. D. Chuang, H. M. Wu
To contact the commercial OPAP-kerosene solution with CH3OH – H20 solution, we used the appropriate concentration of DOPAP / MOPAP solvent. By using this treated OPAP solvent, uranium can be recovered
Jan 1, 1984